浅海采油平台振动原因分析及治理措施
Vibration Cause Analysis of Shallow Water Production Platform and Tre atment Measure
浏览(2219) 下载(1)
- DOI:
- 作者:
- 胡洪勤
HU Hong-qin
- 作者单位:
- 胜利油田胜利工程设计咨询有限责任公司, 山东东营 257026
Shengli Engineering Design Consultation Company of Shengli Oilfie ld, Dongying 257026, China
- 关键词:
- 海洋平台;导管架;振动测试;模拟实验;振动;原因分析
offshore platform;jacket;vibration test;simulative experiment;vibration;cause analysis
- 摘要:
- 针对埕岛油田中心二号生活平台剧烈振动的问题进行研究,通过理论分析、数值计算、模拟实验和现场测试,认为生活平台剧烈振动主要是由于导管架与桩的相对运动引起的。另外,海底冲刷造成导管架泥线处淘空,使导管架在泥线处失去约束,降低了结构的侧向刚度,进而加剧了平台的振动。根据问题产生的原因,采取了灌浆加抛石的治理方案。结果表明,这种方法既消除了导管架与桩的相对运动,又提高了基础的约束作用,最大减振幅度达到89%,实现了预期的减振目标。指出:浅海油田不宜采用直立式非灌浆桩腿导管架平台,平台设计时应考虑淘空的影响,采取相应措施,避免淘空降低平台的侧向刚度。
With the theoretical analysis, numerical calculation, simulative ex periment and field test, the main cause of strong vibration at the living platf orm of Chengdao Oilfield Central Platform No.2 was founded, that was the relati ve movement between jacket and piles. Afterwards, the treatment of using grouti ng and riprap was carried out, and the anticipative object of vibration-reducin g was realized. This method not only eliminated the relative movement between ja cket and piles, but also increased the foundational constraint action. The maxi mum amplitude of vibration was reduced by 89%.2005,3(3): 36-39 收稿日期:2005-3-4分类号:TE54作者简介:胡洪勤(1946-),男,山东临清人,高级工程师,1970年毕业于同济大学,从事港口工程及海洋工程设计.参考文献:
[1]刘锦昆."埕岛二号"中心平台非灌浆腿导管架结构设计[J].中国海洋平台,1999,14(4):23-25.
[2]Huang W P,Jiang J T,Yang Y C. Investigation on the Cause of Excessive Vibration of a Jacket Type Offshore Platforms[A]. The Proceedings of the First ASIAN AND PACIFIC COASTAL ENGINEERING CONFERENCE [ C ].Dalian, China: Dalian University of Technology, 2001. 624-629.
[3]黄维平,杨永春,蒋济同.直立式非灌浆桩腿导管架平台超常态振动研究[J].振动工程学报,2002,15(3):368-371.
[4]黄维平,李华军,刘娟.直立式非灌浆桩腿导管架平台侧向刚度的简化计算[J].工程力学,2002,增刊:797-800.
[5]周长江.极浅海油田开发技术与实践[M].北京:石油工业出版社,2000.
