油田采出水处理工艺改造优化设计
Alteration and Optimizing-design of Oilfield Produced Water Treatment Process
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- DOI:
- 作者:
- 方世跃1,2, 余胜国2, 邹照彰2, 孙莉蓉2, 李能武2, 王洪辉1
Fang Shiyue1,2, Yu Shengguo2, Zou Zhaozhang2, Sun Lirong2, Li Nengrong2, Wang Honghun1
- 作者单位:
- 1. 成都理工大学能源学院, 四川成都 610059;
2. 青海油田采油三厂, 青海芒崖 816400
College of Energy Sources, Chengdu University of Technology, Chengdu 610059, Chi- na
- 关键词:
- 油田注水;油田采出水;水处理工艺;工艺改造
single wall pipe;thermal insulation;weighted;new product;application
- 摘要:
- 文章对柴达木盆地西部花土沟油田50万t联合站的油田采出水处理系统不能正常运行的情况进行了分析,认为其主要原因是由于自然沉降罐和聚结除油器负荷超标、压力过滤罐筛管堵塞、污水储罐及工艺管道腐蚀、化学药剂与来液量不匹配、反应时间不足等造成的,基于此对系统的污泥泵进行了改造,对污水储罐进行了封顶,并对沉降罐进行了扩容,解决了水处理系统不能正常运行的问题,取得了良好的效果。
This paper analyses the problems of the oilfield produced water treatment system at the 50 ×104 t gas-oil treatment station of Huatugou Oilfield, west of Qaidam Basin. The causes were considered as the exceeded loads on the natural sedimentation tank and coalescing deoiler, sieve tube blocking of pressure filter,corrosion of sewage tank and process pipeline, mismatching of chemical and coming fluid volume, and insufficient reaction time. Based on the analysis, the sludge pump of the treatment system was altered and the sewage storage tank was covered with a roof and the sedimentation tank was enlarged to resolve these problems. The alteration work was successful.2009,03(03): 27-29 收稿日期:2008-6-1分类号:TE357.6基金项目:甘肃省科技攻关项目(GS002—A45—063);甘肃省建设科技攻关项目(JK-2000-4)作者简介:方世跃(1975-),男,安徽太湖人,工程师,成都理工大学油气田开发专业在读博士,从事水处理技术研究工作。参考文献:
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